OWNERS OF STRATA PLAN 52843 and PSAROS BUILDERS PTY LTD

Case

[2013] WASAT 46

05/04/2013

No judgment structure available for this case.

Judgment
State Administrative Tribunal
  • Site map
  • |
  • Accessibility
  • |
  • Contact Us
  • Search
  • SAT Home Page
  • Decisions

  • Decisions - last 90 days
  • Decisions with reasons
  • Decisions by Legislation
  • Decisions by Act
  • Orders
  • Previous Board and Tribunal Decisions

  • Equal Opportunity Tribunal
  • Guardianship and Administration Board
  • Strata Titles Tribunal
  • Town Planning Appeal Tribunal
  • Quick Search

  • Advanced Search

  • Advanced Search
  • Help

  • Help
Return to List

OWNERS OF STRATA PLAN 52843 and PSAROS BUILDERS PTY LTD [2013] WASAT 46



STATE ADMINISTRATIVE TRIBUNALCitation No:[2013] WASAT 46
05/04/2013
BUILDING SERVICES (COMPLAINT RESOLUTION and ADMINISTRATION) ACT 2011 (WA)
Case No:CC:602/20128, 9, 11 & 12 OCTOBER AND 6 & 7 DECEMBER 2012
Coram:MS A DAVIES (SENIOR SESSIONAL MEMBER)
MR J FISHER (SENIOR SESSIONAL MEMBER)
MR P MITTONETTE (SESSIONAL MEMBER)
5/04/13
86Judgment Part:1 of 2
Result: Application granted
BOther Parts:Pages 51 to 86
PDF Version
Parties:OWNERS OF STRATA PLAN 52843
PSAROS BUILDERS PTY LTD

Catchwords:

Building Services (Complaint Resolution and Administration) Act 2011 (WA) ­ Whether the Tribunal may grant more than one building remedy order in respect of a regulated building service that has not been carried out in a proper and proficient manner or is faulty or unsatisfactory ­ Whether s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011 (WA) is wide enough to cover circumstances such as where an applicant seeks to be compensated for money already paid to third parties to rectify poor workmanship ­ Whether the regulated building service complained of, namely, construction of the basement and, in particular, waterproofing of the basement, had been carried out in a proper and proficient manner or is faulty or unsatisfactory ­ Whether applicant had a duty to warn principal of non­compliance with Building Code of Australia

Legislation:

Builders Registration Act 1939 (WA)
Builders Registration Act 2011 (WA)
Building Act 2011 (WA)
Building Code of Australia 2006
Building Code of Australia 2007
Building Regulations 1989 (WA), reg 5, reg 10
Building Services (Complaint Resolution and Administration) Act 2011 (WA), s 3, s 5, s 5(1), s 5(1)(2), s 9(1), s 10, s 11(1), s 11(1)(d), s 36(1), s 36(1)(a), s 36(1)(), s 38, s 38(1), s 38(1)(a)
Building Services (Complaint Resolution and Administration) Bill 2010 (WA)
Building Services (Complaint Resolution and Administration) Regulations 2011 (WA), reg 6, reg 6(2), reg 6(3)
Interpretation Act 1984 (WA), s 10(c)
State Administration Tribunal Act 2004 (WA), s 9, s 32(1), s 32(2), s 32(4), s 34(1), s 83

Case References:

Atkinson and Rio Vista Pty Ltd trading as Freedom Pools and Spas [2012] WASAT 116
Brodun Construction and Love [2008] WASAT 174
Cable Limited and Hutcherson Bros Pty Limited (1969) 123 CLR 143; [1969] HCA 37
Codelfa Construction Pty Ltd v State Rail Authority of NSW [1982] HCA 24; (1982) 149 CLR 337
Henry Michael Lyons & Ors v Jandon Constructions (A Firm) & Ors [1998] WASC
Owners of Strata Plan no 47111 v Pyramid Constructions Pty Ltd [2012] WASAT 79
Personal Representatives of Tang Man Sit v Capacious Investments Ltd [1996] 1 AC 514
Re Griffiths; Ex Parte Homestyle Pty Ltd [2005] WASCA 103
Re McGuire; ex parte Bradshaw (Unreported, Supreme Court, 30 April 1986, Lib No 6260A-C
Western Export Services Inc v Jireh International Pty Ltd [2011] HCA 45


Orders

On the application heard on 8, 9, 11 & 12 October 2012 and 6 & 7 December 2012, by Senior Sessional Member Abigail Davies, Senior Sessional Member John Fisher and Sessional Member Peter Mittonette, it is on 5 April 2013 ordered that:  ,1. The respondent must pay the applicant $76,477 within 28 days of the date of this order.,2. The respondent is to remedy the ingress of water into the basement carpark at Tyne Square in accordance with option 1 of the Joint Expert Recommendations dated 10 October 2012 within six months of the date of this order or such further date as the Tribunal orders.,3. Compliance with order 2 is subject to completion of a duly certified design by a structural engineer and written agreement to the certified design by the applicant.,4. Compliance with order 2 may require some development of option 1 to ensure compliance with all relevant laws, regulations and requirements, including, for example, minimum height requirements.  If this cannot be resolved by agreement between the parties, each party has liberty to apply on seven days' notice.,5. The respondent is to make good areas affected by the remedial work.

Summary

This dispute concerned water ingress into the northern part of the basement car park of a mixed use development at 154 Newcastle Street, Perth (Tyne Square) built by the respondent, Psaros Builders Pty Ltd.,The applicant, the Owners of Strata Plan 52843, who are the owners of Tyne Square, sought a building remedy order under s 36(1)(a) of the Building Services (Complaint Resolution and Administration) Act 2011 (WA) that the respondent remedy the basement carpark by, inter alia, the installation of a secondary concrete floor slab, and that the respondent pay the applicant compensation under s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011in the sum of $76,477 for interim remedial works already undertaken by the applicant. ,The hearing was held over six days on 8, 9, 11 and 12 October and 6 and 7 December 2012.,Before turning to address the legal issues for determination in the case, the Tribunal made factual findings relating to:,a) the three roles of Mr Danny Psaros and the construction contract;,b) the development of the design of the basement and waterproofing;,c) how and why water had ingressed the basement;,d) the areas of the basement where water had ingressed and the extent of the problem;,e) the evidence as to what 'a competent builder' would have done with respect to the relief vents;,f) what had been done to-date to remedy aspects of the problem; and,g) what the experts proposed as possible solutions.,Regarding how and why water has ingressed the basement, the Tribunal found that, inter alia, it was more likely than not that a cause of water ingress into the northern part of the basement carpark was rainfall running into the soakwells along the northern wall of the building, which then led to groundwater in the immediate vicinity of the soakwells rising up past the height of the basement floor. The Tribunal also found that while it had not been established that regional groundwater, as distinct from groundwater in the immediately vicinity, had risen up past the height of the basement slab to­date, there has been, and continued to be, a risk that regional groundwater will rise up past the height of the basement slab and ingress the whole of the basement carpark, even if all stormwater was routed off site.,The first legal issue addressed by the Tribunal was whether the Tribunal has jurisdiction to determine this application and power to grant the remedies sought. The Tribunal considered principles of statutory interpretation, including the purpose of the Building Services (Complaint Resolution and Administration) Act 2011, and found that it has the power to grant more than one building remedy order in respect of a regulated building service that has not been carried out in a proper and proficient manner or is faulty or unsatisfactory. The Tribunal also considered that the ordinary and natural meaning of the term 'compensation' in s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011 is wide enough to cover circumstances such as where the applicant seeks to be compensated for money already paid to third parties to rectify poor workmanship, and found that the Tribunal has the power to grant an award of money under s 36(1)(c) of the Act in respect of interim remedial works already undertaken at the direction of the applicant.,The second legal issue addressed by the Tribunal was whether the regulated building service complained of ­ namely, the construction of the basement and, in particular, the waterproofing of the basement ­ had been carried out in a proper and proficient manner or is faulty or unsatisfactory. ,The Tribunal did not accept the respondent's position that it was not responsible for the water ingress into the basement because it was not responsible for the design of the building and that it merely constructed Tyne Square in accordance with the construction contract.,The Tribunal found that the puncturing by the respondent of a vapour barrier installed under the basement slab in constructing the relief vents amounted to a failure by the respondent to carry out the building service in a proper and proficient manner and that the vapour barrier was thereby rendered faulty and unsatisfactory within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011. In reaching this conclusion, the Tribunal relied principally on the nature of the alleged defect, the expert evidence including as to what would have been immediately apparent to a competent builder, the fact that the respondent was responsible under the construction contract for the implementation and performance of the waterproofing of the basement and the respondent's failure to comply with the Building Code of Australia. The Tribunal considered that relying on consultants whose objective was to achieve other aspects of design, and who were not responsible for waterproofing, in order to ensure that the waterproofing in all respects was satisfactory, amounted to an error of judgment by Mr Psaros as the controlling mind of the respondent.,The Tribunal also found that, at least by 2 May 2007, the respondent was required under the construction contract to proceed to warn the principal of the non­compliance or risk of non­compliance with FP1.5 of the Building Code of Australia and that it did not do so. In the circumstances of this case, the contractual requirement to warn formed part of the building service under s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011, as it was necessary preparatory work involved in the builder's work, and this failure also amounted to a failure to carry out the building service in a proper and proficient way within the meaning of s 38(1) of the Act. ,Further, the Tribunal did not accept Mr Psaros' argument that all the construction contract required for waterproofing under the basement was the installation of a vapour barrier. The Tribunal considered that, upon a proper construction of the construction contract, the 'underlay' in the Specifications should not have been selected, as it does not appear in the Plans and the 'waterproofing' in the Plans required the respondent to have selected one of the possible types of waterproofing set out under 'Water Proof Membrane Systems'. The Tribunal therefore also found that installation of the vapour barrier instead of one of the possible types of waterproofing set out under 'Water Proof Membrane Systems' in the Specifications amounted to a failure to carry out the building services in a proper or proficient manner within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011 in that no conventional form of waterproofing has been installed at all.,Further, based on the expert evidence, the Tribunal found that, whether or not the vapour barrier itself had yet failed, it was an inadequate and unacceptable device to exclude water, given the risk that regional groundwater could rise up to RL 10.5 AHD at a certain point or points in time. As such, the vapour barrier was also faulty and unsatisfactory within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011. The fact that groundwater had only risen in the immediate vicinity of the northern part of Tyne Square, and highlighted this inadequacy which might otherwise may never have been highlighted, does not itself prevent a conclusion of poor workmanship. ,Further, the Tribunal found that the failure to insert an external waterstop at the joint between the AFS wall and the basement floor in the circumstances of Tyne Square amounted to a failure by the respondent to carry out a building service in a proper and proficient manner within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011, in that a vapour barrier was selected as the device to exclude water, thereby rendering additional sealing of this joint necessary, and an external waterstop was not provided by the respondent. The construction contract expressly stated that the respondent was responsible for the performance of the waterproofing, including for omissions. ,Further, the Tribunal found that the failure to seal the cable entry points into the transformer room and switchboard room and to install a waterstop at the joint between the wall and basement floor at that location amounted to failure to carry out a regulated building service in a proper or proficient manner and that the cable entry points and joints were faulty and unsatisfactory within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011. Regarding the failure to seal the cable entry points, it is an obvious and extreme example of poor workmanship by a builder to build a waterproof service room and then build large holes into that room through which cables are fed, without also resolving the sealing of those large holes. Regarding the joint between the wall and basement floor at the location of the transformer room and switchboard room, the Tribunal accepted expert opinion that in the circumstances of Tyne Square the failure constituted poor workmanship by the respondent. ,The applicant did not establish that the grade of the basement around the relief vents was faulty or unsatisfactory, nor that the construction contract had not been complied with in the installation of waterproofing up the walls.,The third legal issue addressed by the Tribunal was, if any aspect or aspects of the regulated building service has not been carried out in a proper and proficient manner or is faulty or unsatisfactory, what is the appropriate remedy. The Tribunal found that the sum of $76,477, including GST, compensated the applicant within the meaning of s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011, to the extent of the costs claimed, for the respondent's failure to completely waterproof the transformer room and switchboard room, including by reason of the risk that, if water were to rise up to RL 10.5 AHD, water will ingress into the trenches in the transformer room and switchboard room from water flowing over the basement floor.,The Tribunal also found that it was reasonable and appropriate to require the respondent to remedy the basement carpark by, inter alia, the installation of a secondary concrete floor slab, including because the costs involved in respect of the three options are similar when viewed over the longer term, and this option is the only option that enables the punctures created by the relief vents to be fixed so that the mechanism to exclude water is effective. ,When making an order under s 36(1)(a) of the Building Services (Complaint Resolution and Administration) Act 2011, the Tribunal does not ordinarily specify a method of rectification. However, in the circumstances of Tyne Square, the Tribunal considered it appropriate to do so.

JURISDICTION : STATE ADMINISTRATIVE TRIBUNAL STREAM : COMMERCIAL & CIVIL ACT : BUILDING SERVICES (COMPLAINT RESOLUTION and ADMINISTRATION) ACT 2011 (WA) CITATION : OWNERS OF STRATA PLAN 52843 and PSAROS BUILDERS PTY LTD [2013] WASAT 46 MEMBER : MS A DAVIES (SENIOR SESSIONAL MEMBER)
    MR J FISHER (SENIOR SESSIONAL MEMBER)
    MR P MITTONETTE (SESSIONAL MEMBER)
HEARD : 8, 9, 11 & 12 OCTOBER AND 6 & 7 DECEMBER 2012 DELIVERED : 5 APRIL 2013 FILE NO/S : CC 602 of 2012 BETWEEN : OWNERS OF STRATA PLAN 52843
    Applicant

    AND

    PSAROS BUILDERS PTY LTD
    Respondent

Catchwords:

Building Services (Complaint Resolution and Administration) Act 2011 (WA) ­ Whether the Tribunal may grant more than one building remedy order in respect of a regulated building service that has not been carried out in a proper and proficient manner or is faulty or unsatisfactory ­ Whether s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011 (WA) is wide enough to cover circumstances such as where an applicant seeks to be



(Page 2)

compensated for money already paid to third parties to rectify poor workmanship ­ Whether the regulated building service complained of, namely, construction of the basement and, in particular, waterproofing of the basement, had been carried out in a proper and proficient manner or is faulty or unsatisfactory ­ Whether applicant had a duty to warn principal of non­compliance with Building Code of Australia

Legislation:

Builders Registration Act 1939 (WA)


Builders Registration Act 2011 (WA)
Building Act 2011 (WA)
Building Code of Australia 2006
Building Code of Australia 2007
Building Regulations 1989 (WA), reg 5, reg 10
Building Services (Complaint Resolution and Administration) Act 2011 (WA), s 3, s 5, s 5(1), s 5(1)(2), s 9(1), s 10, s 11(1), s 11(1)(d), s 36(1), s 36(1)(a), s 36(1)(), s 38, s 38(1), s 38(1)(a)
Building Services (Complaint Resolution and Administration) Bill 2010 (WA)
Building Services (Complaint Resolution and Administration) Regulations 2011 (WA), reg 6, reg 6(2), reg 6(3)
Interpretation Act 1984 (WA), s 10(c)
State Administration Tribunal Act 2004 (WA), s 9, s 32(1), s 32(2), s 32(4), s 34(1), s 83

Result:

Application granted


Summary of Tribunal's decision:

This dispute concerned water ingress into the northern part of the basement car park of a mixed use development at 154 Newcastle Street, Perth (Tyne Square) built by the respondent, Psaros Builders Pty Ltd.


The applicant, the Owners of Strata Plan 52843, who are the owners of Tyne Square, sought a building remedy order under s 36(1)(a) of the Building Services (Complaint Resolution and Administration) Act 2011 (WA) that the respondent remedy the basement carpark by, inter alia, the installation of a secondary concrete floor slab, and that the respondent pay the applicant compensation under s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011in the sum of $76,477 for interim remedial works already undertaken by the applicant.

(Page 3)

The hearing was held over six days on 8, 9, 11 and 12 October and 6 and 7 December 2012.
Before turning to address the legal issues for determination in the case, the Tribunal made factual findings relating to:
a) the three roles of Mr Danny Psaros and the construction contract;
b) the development of the design of the basement and waterproofing;
c) how and why water had ingressed the basement;
d) the areas of the basement where water had ingressed and the extent of the problem;
e) the evidence as to what 'a competent builder' would have done with respect to the relief vents;
f) what had been done to-date to remedy aspects of the problem; and
g) what the experts proposed as possible solutions.
Regarding how and why water has ingressed the basement, the Tribunal found that, inter alia, it was more likely than not that a cause of water ingress into the northern part of the basement carpark was rainfall running into the soakwells along the northern wall of the building, which then led to groundwater in the immediate vicinity of the soakwells rising up past the height of the basement floor. The Tribunal also found that while it had not been established that regional groundwater, as distinct from groundwater in the immediately vicinity, had risen up past the height of the basement slab to­date, there has been, and continued to be, a risk that regional groundwater will rise up past the height of the basement slab and ingress the whole of the basement carpark, even if all stormwater was routed off site.

The first legal issue addressed by the Tribunal was whether the Tribunal has jurisdiction to determine this application and power to grant the remedies sought. The Tribunal considered principles of statutory interpretation, including the purpose of the Building Services (Complaint Resolution and Administration) Act 2011, and found that it has the power to grant more than one building remedy order in respect of a regulated building service that has not been carried out in a proper and proficient manner or is faulty or unsatisfactory. The Tribunal also considered that the ordinary and natural meaning of the term 'compensation' in s 36(1)(c) of the Building Services (Complaint Resolution and Administration) Act 2011 is wide enough to cover circumstances such as where the applicant seeks to be compensated for money already paid to third parties to rectify poor workmanship, and found that the Tribunal has the power to grant an award of money under s 36(1)(c) of the Act in respect of interim remedial works already undertaken at the direction of the applicant.
The second legal issue addressed by the Tribunal was whether the regulated building service complained of ­ namely, the construction of the basement and, in particular, the waterproofing of the basement ­ had been carried out in a proper and proficient manner or is faulty or unsatisfactory.

(Page 4)

The Tribunal did not accept the respondent's position that it was not responsible for the water ingress into the basement because it was not responsible for the design of the building and that it merely constructed Tyne Square in accordance with the construction contract.
The Tribunal found that the puncturing by the respondent of a vapour barrier installed under the basement slab in constructing the relief vents amounted to a failure by the respondent to carry out the building service in a proper and proficient manner and that the vapour barrier was thereby rendered faulty and unsatisfactory within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011. In reaching this conclusion, the Tribunal relied principally on the nature of the alleged defect, the expert evidence including as to what would have been immediately apparent to a competent builder, the fact that the respondent was responsible under the construction contract for the implementation and performance of the waterproofing of the basement and the respondent's failure to comply with the Building Code of Australia. The Tribunal considered that relying on consultants whose objective was to achieve other aspects of design, and who were not responsible for waterproofing, in order to ensure that the waterproofing in all respects was satisfactory, amounted to an error of judgment by Mr Psaros as the controlling mind of the respondent.
The Tribunal also found that, at least by 2 May 2007, the respondent was required under the construction contract to proceed to warn the principal of the non­compliance or risk of non­compliance with FP1.5 of the Building Code of Australia and that it did not do so. In the circumstances of this case, the contractual requirement to warn formed part of the building service under s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011, as it was necessary preparatory work involved in the builder's work, and this failure also amounted to a failure to carry out the building service in a proper and proficient way within the meaning of s 38(1) of the Act.
Further, the Tribunal did not accept Mr Psaros' argument that all the construction contract required for waterproofing under the basement was the installation of a vapour barrier. The Tribunal considered that, upon a proper construction of the construction contract, the 'underlay' in the Specifications should not have been selected, as it does not appear in the Plans and the 'waterproofing' in the Plans required the respondent to have selected one of the possible types of waterproofing set out under 'Water Proof Membrane Systems'. The Tribunal therefore also found that installation of the vapour barrier instead of one of the possible types of waterproofing set out under 'Water Proof Membrane Systems' in the Specifications amounted to a failure to carry out the building services in a proper or proficient manner within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011 in that no conventional form of waterproofing has been installed at all.

(Page 5)

Further, based on the expert evidence, the Tribunal found that, whether or not the vapour barrier itself had yet failed, it was an inadequate and unacceptable device to exclude water, given the risk that regional groundwater could rise up to RL 10.5 AHD at a certain point or points in time. As such, the vapour barrier was also faulty and unsatisfactory within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011. The fact that groundwater had only risen in the immediate vicinity of the northern part of Tyne Square, and highlighted this inadequacy which might otherwise may never have been highlighted, does not itself prevent a conclusion of poor workmanship.
Further, the Tribunal found that the failure to insert an external waterstop at the joint between the AFS wall and the basement floor in the circumstances of Tyne Square amounted to a failure by the respondent to carry out a building service in a proper and proficient manner within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011, in that a vapour barrier was selected as the device to exclude water, thereby rendering additional sealing of this joint necessary, and an external waterstop was not provided by the respondent. The construction contract expressly stated that the respondent was responsible for the performance of the waterproofing, including for omissions.
Further, the Tribunal found that the failure to seal the cable entry points into the transformer room and switchboard room and to install a waterstop at the joint between the wall and basement floor at that location amounted to failure to carry out a regulated building service in a proper or proficient manner and that the cable entry points and joints were faulty and unsatisfactory within the meaning of s 38(1) of the Building Services (Complaint Resolution and Administration) Act 2011. Regarding the failure to seal the cable entry points, it is an obvious and extreme example of poor workmanship by a builder to build a waterproof service room and then build large holes into that room through which cables are fed, without also resolving the sealing of those large holes. Regarding the joint between the wall and basement floor at the location of the transformer room and switchboard room, the Tribunal accepted expert opinion that in the circumstances of Tyne Square the failure constituted poor workmanship by the respondent.
The applicant did not establish that the grade of the basement around the relief vents was faulty or unsatisfactory, nor that the construction contract had not been complied with in the installation of waterproofing up the walls.
The third legal issue addressed by the Tribunal was, if any aspect or aspects of the regulated building service has not been carried out in a proper and proficient manner or is faulty or unsatisfactory, what is the appropriate remedy. The Tribunal found that the sum of $76,477, including GST, compensated the applicant within the meaning of s 36(1)(c) of the Building Services (Complaint

(Page 6)

Resolution and Administration) Act 2011, to the extent of the costs claimed, for the respondent's failure to completely waterproof the transformer room and switchboard room, including by reason of the risk that, if water were to rise up to RL 10.5 AHD, water will ingress into the trenches in the transformer room and switchboard room from water flowing over the basement floor.
The Tribunal also found that it was reasonable and appropriate to require the respondent to remedy the basement carpark by, inter alia, the installation of a secondary concrete floor slab, including because the costs involved in respect of the three options are similar when viewed over the longer term, and this option is the only option that enables the punctures created by the relief vents to be fixed so that the mechanism to exclude water is effective.
When making an order under s 36(1)(a) of the Building Services (Complaint Resolution and Administration) Act 2011, the Tribunal does not ordinarily specify a method of rectification. However, in the circumstances of Tyne Square, the Tribunal considered it appropriate to do so.

Category: B


Representation:

Counsel:


    Applicant : Mr AW Buchan
    Respondent : Mr PG McGowan

Solicitors:

    Applicant : Hotchkin Hanly
    Respondent : Metaxas & Hager



Case(s) referred to in decision(s):

Atkinson and Rio Vista Pty Ltd trading as Freedom Pools and Spas [2012] WASAT 116
Brodun Construction and Love [2008] WASAT 174
Cable Limited and Hutcherson Bros Pty Limited (1969) 123 CLR 143; [1969] HCA 37
Codelfa Construction Pty Ltd v State Rail Authority of NSW [1982] HCA 24; (1982) 149 CLR 337

(Page 7)

Henry Michael Lyons & Ors v Jandon Constructions (A Firm) & Ors [1998] WASC
Owners of Strata Plan no 47111 v Pyramid Constructions Pty Ltd [2012] WASAT 79
Personal Representatives of Tang Man Sit v Capacious Investments Ltd [1996] 1 AC 514
Re Griffiths; Ex Parte Homestyle Pty Ltd [2005] WASCA 103
Re McGuire; ex parte Bradshaw (Unreported, Supreme Court, 30 April 1986, Lib No 6260A-C
Western Export Services Inc v Jireh International Pty Ltd [2011] HCA 45


(Page 8)
REASONS FOR DECISION OF THE TRIBUNAL:

Introduction

1 This dispute concerns water ingress into part of the basement carpark of a mixed use development comprising 83 residential apartments and four commercial units at No 154 Newcastle Street, Perth (Tyne Square).

2 The basement comprises car parking space, store rooms for use of the residents, service rooms for infrastructure for the building (including a transformer room and a switchboard room) and a lift.

3 The finished floor level of the basement ranges from between 5.25 metres below street level, at the junction of Lindsay and Newcastle Streets, to 2.51 metres below street level at the junction of Lindsay Street and the residential boundary.

4 Tyne Square was built by Psaros Builders Pty Ltd (respondent) which is a registered builder. The Owners of Strata Plan 52843 (applicant) are the owners of Tyne Square and seek building remedy orders pursuant to s 36(1) of the Building Services (Complaint Resolution and Administration) Act 2011 (WA) (BS(CRA) Act). Unless otherwise stated, all references to legislation in this decision are to the BS(CRA) Act.

5 The Tribunal is required to act in accordance with equity, good conscience and the substantial merits of the case, without regard to technicalities and legal forms. The Tribunal is bound by the rules of natural justice except to the extent that the State Administrative Tribunal Act2004 (WA) (SAT Act) or the enabling Act authorises, whether expressly or by implication, a departure from those rules. The Tribunal may inform itself on any matter as it sees fit. The Tribunal is not bound by the rules of evidence or any practices or procedures applicable to courts of record, except to the extent that they are adopted (s 9, s 32(1), s 32(2) and s 32(4) of the SAT Act).

Issues as identified by the parties


6 The hearing was held over six days on 8, 9, 11 and 12 October and 6 and 7 December 2012. There was no statement of issues, facts and contentions.

7 In the applicant's opening address, it alleged that the basement leaks; that is, the basement allows water to ingress into it. The applicant alleged that the respondent did not construct the basement carpark of Tyne Square


(Page 9)
    in a proper and proficient manner and that the building work carried out is faulty and unsatisfactory contrary to s 38(1) in that:

      1) the respondent did not exercise an appropriate degree of independent judgment, as informed by external standards such as the Building Code, in adopting the design of the building work or particular method of construction;

      2) the respondent played an active role in the design process and the manner in which the design came to be adopted, which led directly to the water ingress now occurring; and

      3) the respondent did not complete the work in accordance with its obligations under the construction contract or in accordance with sound building practice.

8 On this basis, the applicant contended it was entitled to an order under s 36(1) requiring the respondent to rectify the basement in accordance with the applicant's experts' recommendations.

9 The applicant also sought recovery of the costs of interim remedial work that had already been undertaken by the applicant.

10 The respondent denied that the applicant was entitled to any relief on the basis that it is not responsible for the design of the building work and that it constructed Tyne Square in accordance with the construction contract.

11 The respondent stated that it accepted that, simply because responsibility for design might lie with a consultant rather than with the contracting builder, does not, in each and every case, lead to the result that the builder can blindly hide behind the lack of contractual relationship or responsibility allocated to others. However, in the present case, the respondent contended the design decision that gave rise to the decision to install what are referred to, in this decision, as the relief vents into the concrete slab and thereby permit water to ingress into the basement, was a decision for which the hydraulics consultant and the structural engineer, neither of whom had been retained by the respondent, were responsible.

12 The respondent also submitted in closing submissions that to find, in the circumstances of this case, that the respondent is liable would have the effect of turning the builder into a guarantor of decisions made by others who, in each case, have expertise not held by the builder,


(Page 10)
    and that such a finding, as a precedent, would be both dangerous and alarming.




Preliminary findings


A. The three roles of Mr Danny Psaros and the construction contract

13 There is no contractual relationship between the applicant and the respondent.

14 By joint venture agreement dated 5 August 2005 (JVA), Psaros Property Group Pty Ltd (PPG) and Pakwest Pty Ltd (Pakwest), a company controlled by Mr Luke Saraceni, constituted themselves as an unincorporated joint venture (JV) to undertake the construction of what is now known as Tyne Square.

15 Under the JVA, it was agreed that PPG had a one­third interest and Pakwest had a two­third interest in the JV, with the parties to share the profits and losses (if any) and contribute equity in the same proportions.

16 It was agreed that if the Tyne Square project proceeded to construction, PPG would be engaged by the JV to act as Project Manager for a fee of $300,000, plus GST, from the date the parties agree to proceed or from the date of approval of finance, whichever was later. It was also agreed that PPG would provide submissions, as the proposed builder, of a price to carry out the construction on a 'cost plus 10% basis' and that PPG would be engaged to carry out the construction, subject to Pakwest being satisfied as to the price proposed by PPG, and if not so satisfied, another builder would be engaged.

17 An agreement supplemental to the JVA and dated 1 February 2007 was also entered into by PPG and Pakwest. Recital B of that supplemental agreement provides that the builder to be engaged by the JV will be a related entity of PPG nominated by PPG.

18 PPG was paid $15,000, plus GST, per month for project management services from April 2006 until November 2007.

19 There is no documentary evidence specifying the tasks of PPG in acting as Project Manager.

20 Consultants were engaged by Mr Psaros on behalf of the JV through PPG or Psaros Constructions Pty Ltd (not Psaros Builders Pty Ltd) including:


(Page 11)
    a) Overman & Zuideveld Pty Ltd (Architects) to develop the design of the construction and to integrate the work of specialist consultants with the architectural drawings;

    b) Golder Associates Pty Ltd (Golder) through Mr Fred Davenport to undertake geotechnical investigation and soil assessment on site;

    c) Pipeline Hydraulics Pty Ltd (Pipeline Hydraulics) to provide hydraulic consulting services including the design of all rainwater disposal services and sanitary drains, wastes and vents; and

    d) Saraceni Engineering Group Pty Ltd (SEG) to provide structural engineering services including in design development, documentation and construction.


21 Mr Psaros is a director and the chief executive officer (CEO) of, inter alia, both the respondent and PPG. In the context of the construction of Tyne Square, therefore, Mr Psaros had three roles. He was a one­third owner/developer through PPG, a 'Project Manager' on behalf of the JV, also through PPG, and the builder through the respondent.

22 It appears that Mr Psaros shared the role of builder with his business partner, Mr Robert De Francesh (T:317, 325 and 326; 12.10.12). However, it was Mr Psaros who was the registered individual builder behind the respondent (T:112; 11.10.12).

23 Mr Psaros obtained a Certificate in Architectural Drafting in 1977 and a Diploma in Architectural Drafting in 1979 from Leederville Technical College. He qualified as a registered builder in 1986.

24 The applicant submitted, in relation to Mr Psaros as a witness, inter alia, that the evidence of Mr Psaros did not have a ring of truth to it and that he took a wilfully evasive and obfuscating approach to the giving of his evidence. The applicant also submitted that the evidence of Mr Psaros should be treated with extreme caution due to the manner in which Mr Psaros gave his evidence and numerous omissions and inconsistencies demonstrated by his evidence, some of which the applicant outlined.

(Page 12)



25 Mr Psaros appeared to be very stressed to be in the witness box for what the Tribunal accepts was the first time he had given evidence (T:119; 11.10.12). He genuinely did not appear to completely understand the place cross­examination has in the process of determination; rather, he repeatedly tried to tell his side of the story. He seemed focused on communicating to the Tribunal that it was the consultants whose advice dictated the design of Tyne Square and he had his own views about why there has been water ingress into the basement. This often coloured his answers to questions put to him. There were also times when Mr Psaros contradicted himself or did not give clear answers. The Tribunal does conclude, for all of these reasons, that Mr Psaros' evidence must be treated with considerable caution. The Tribunal does not, however, accept the applicant's submission that Mr Psaros was wilfully obfuscating in his evidence.

26 The Tribunal finds that the respondent constructed Tyne Square pursuant to a contract dated 8 March 2007 between the respondent, defined therein as contractor, and PPG and Pakwest, defined therein as principal (Contract).

27 The Tribunal does not accept Mr Psaros' evidence which suggests that this document, now defined as the Contract, was merely 'to do with bank financing arrangements' (T:297 and 298; 12.10.12), although, as evidenced by Exhibit R, a similar contract would appear to have been sent to the joint venturers' bank.

28 The document tabled by Mr Psaros at a meeting with Mr Luke Saraceni of Pakwest on 5 October 2009 described the Contract as 'not appropriate'. However, having been duly executed, the Contract is legally binding on the parties to it.

29 The Contract includes AS 2124 general terms and conditions, the various approved versions of plans at Exhibit A, pages 339 - 378 (an A1 version of these plans is at Exhibit W) (Plans) and the specifications dated April 2007 at Exhibit A, pages 152 - 306 (Specifications). Sixteen pages, being 135 - 199, are missing from Exhibit B, but these can be found at Exhibit A, pages 75 ­ 140.

30 The Formal Instrument of Agreement evidencing execution is at Exhibit B16, page 199.

31 The Contract commenced on 12 March 2007 (clause 35.1 of the Contract at Exhibit B16, pages 104 and 105, and Exhibit U), and practical completion was on 17 July 2009.

(Page 13)



32 The Specifications, which are dated April 2007, refer, at page 6, to AS 2124 being part of the Contract documents, but it was not until some two years later that AS 2124 general terms and conditions, as amended, was formally executed and backdated to 8 March 2007.

33 Under the Contract, the respondent was required to complete the work for the contract sum. 'Contract sum' is defined to be a lump sum and/or rates, whichever is accepted by the principal, but may also include provisional sums. In this instance, unusually for this type of contract, the contract sum constituted (by reason of the amendment at Exhibit B16, page 196) the 'provisional sum' at Exhibit B16, page 198, as finally determined pursuant to the Contract.

34 Pursuant to clause 11 of the Contract, a provisional sum shall not, itself, be payable, but where, at the direction of the superintendent, the work to which the provisional sum relates is performed or supplied by the contractor, the work is to be valued under clause 40.5 of the Contractdealing with valuation of variations. If the work is performed or supplied by a subcontractor, clauses 11(b) and 11(c) apply, and the Contract provides, in the annexure, for the contractor to be paid 10% for profit and attendance.

35 Further, variations directed by the superintendent under clause 40.1 of the Contract, dealing with variations to work, could be carried out and valued as daywork under clause 41.

36 Pursuant to clause 8, the several documents forming the Contract are to be taken as mutually explanatory of one another. If either party discovers any ambiguity or discrepancy in any document prepared for the purpose of executing the work under the Contract, that party shall notify the superintendent in writing of the ambiguity or discrepancy. The superintendent shall then direct the contractor as to the interpretation to be followed by the contractor in carrying out the work.

37 Pursuant to clause 14 of the Contract, the contractor was required to comply with the requirements, inter alia, of:


    • acts and ordinances of the State or Territory in which the work under the Contract is carried out;

    • ordinances, regulations, by-laws, orders and proclamations under the acts; and


(Page 14)
    • ordinances and persons acting in exercise of statutory powers enabling them to give directions affecting the work under the Contract.
    If a requirement is at variance with a provision of the Contract, as soon as the contractor discovers the variance, the contractor shall notify the superintendent in writing specifying the difference. If so, the superintendent shall direct a variation.

38 The law governing the Contract and its interpretation is the law of Western Australia.

39 The superintendent under the Contract was Mr Frank Saraceni. Mr Frank Saraceni was a director of the consulting engineers, SEG. He is also the brother of Mr Luke Saraceni.

40 The Plans and Specifications also specify various Australian Standards (AS) in accordance with which the corresponding part of the work is to be built.

41 The AS 2124 form of contract can loosely be described as a 'construct only' form of contract, as distinct from a contract under which a builder contracts to 'design and construct' a building.

42 Part of the respondent's defence of the applicant's claim was that the contractual relationship between the respondent and the principal under the Contract was a 'construct only' and not 'design and construct' and that, while a builder cannot blindly hide behind a lack of contractual relationship with an applicant, in these circumstances, the respondent could not be held responsible for any design defects. The respondent submitted that the design underpinning that about which the applicant complains was a design for which Pipeline Hydraulics was contractually responsible and for which, in all senses, it and probably the structural engineer were responsible (T:54 and 55; 08.10.12).

43 The Tribunal does not accept these submissions in that they do not address squarely the builder's responsibility under the BS(CRA) Act in constructing Tyne Square.

44 A 'construct only' type of contract does not have any specific meaning in law and nor does the term 'design'. The precise parameters of legal responsibility, including relating to aspects of design, are determined by the specific words of a contract, which must be interpreted within the context of the contract as a whole. Even in contracts that can be described as 'construct only', aspects of construction may be left


(Page 15)
    to the builder which may involve aspects that can be characterised as 'design'. Clause 16.3(f) of the Contract expressly recognises that an aspect of design may be provided by the contractor. Clause 10.4 of the Contract requires that, if the contractor is to be responsible for an aspect of design, the responsibility shall be expressly stated in the Contract.

45 In the present case, 'work under the Contract' is defined in clause 2 of the Contract to mean the work which the contractor is or may be required to execute under the Contract, including variations, remedial work, construction plant and temporary work. In this Contract, the work to be performed by the respondent is set out in the Plans and Specifications.

46 Relevantly, the Specifications, at page 57 in the 'Concrete' section, under 'Part II Materials', provide as follows (Exhibit A, page 208):


    UNDERLAYS, MEMBRANES

    SLABS ON GROUND

    REQUIREMENT: Provide a layer of waterproof film underlay as specified herein.

    FILM UNDERLAY

    MATERIAL: High-impact resistant polyethylene film, to AS 1326.

    Thickness:….200microns

    INSTALLATION: Lay over the base. Lap joints not less than 200mm. Face the laps away from the direction of concrete pour. Seal laps with approved pressure-sensitive adhesive tape. Similarly seal around penetrations such as service pipes and the like. Take the underlay up vertical faces and as detailed on the drawings.

    WATER PROOF MEMBRANE SYSTEMS -

    SHEET MEMBRANES:

    Bituminous multilayer systems: To the relevant requirements of AS CA55.

    Single layer systems: Sheets fixed and lapped with appropriate adhesive or heat welded by gas torch ('torch on').

    SEAMLESS MEMBRANES: Membranes applied in liquid or gel form and air cured to form a seamless film.


(Page 16)
    SUBSTRATES FOR MEMBRANES: Apply the membrane to dry, smooth, firm, continuous surfaces, clean and free from loose or foreign matter. Provide coving or fillets on internal corners. Round or arris external corners and edges.

    Dryness test for substrate: To AS 1884 Appendix A.

    MEMBRANE PROTECTION: Protect the membrane after installation with a permanent protective boarding. Use a low melt bitumen or suitable solvent free adhesive to adhere the protection boards to the membrane with maximum 6 mm gap at joints in the boards.

    APPROVAL OF MEMBRANE SYSTEM:

    Submit proposal together with complete technical information for the water proof membrane system to the Engineer for approval before use. The approval of the systems shall not relieve the Contractor from full responsibility for the performance and installation of the system and from mistakes or omissions or for any discrepancy or deviation from the Specification and other drawings.

    BITUMOUS COATING -

    MATERIAL: Rubber-fortified water-based bitumen emulsion.

    APPLICATION: To clean dry surfaces, by brush or spray, in three coats, to the following coverages:

    First coat: 1.7 L/m2


    Second coat: 2.0 L/m2
    Third coat: 2.0 L/m2[.]
47 Similarly, in the 'Tanking' section under 'Part I, General' at page 96 of the Specifications, which includes the locations and types of certain waterproof membranes to be installed, it is provided, inter alia, that:

    [the]Builder [is] to confirm method of waterproofing basement prior to proceeding with construction.

    Provide to the Proprietor a warranty, for a period of ten years from the date of Practical Completion, covering the whole of the tanking including penetrations for pipes, flues, upstands, flashings and the like. (Exhibit A, page 247).


48 Also, for example, in SEG's issued 'Concrete Details' plans S201 revision 7, there is a note at Section A and at Section B:
(Page 17)
    De-Watering and tanking proposal to be submitted to Engineer prior to works commencing. (Exhibit A, page 340)

49 In interpreting contracts, it is the objective intention of the parties as expressed in the document that is to be determined; See Codelfa Construction Pty Ltd v State Rail Authority of NSW [1982] HCA 24; (1982) 149 CLR 337 (Codelfa); Western Export Services Inc v Jireh International Pty Ltd [2011] HCA 45.

50 The effect of the provisions extracted above, within the Contract as a whole, includes the following:


    1) to the extent that a type and method of waterproofing is detailed in the Contract, the respondent was contractually obliged to the principal to comply with those details;

    2) the respondent was required to submit the proposal of a waterproof membrane system to the engineer before installation; and

    3) approval of the waterproof membrane system did not relieve the respondent from full responsibility for the installation and performance of the system, even if approved by the principal's consultants.


51 Contrary to Mr Psaros' assertion, the supplemental agreement to the JVA dated 1 February 2007 does not 'override ... everything else' (T:298; 12.10.12). The Tribunal does not accept Mr Psaros' assertion that the Contract is a 'cost­plus' contract (T:127; 11.10.12). It is a lump sum contract in which the ‘provisional sum’ provisions have been used. Whether or not the Contract might be described as having 'cost­plus' elements within it, the work to be performed and the final Contract Sum is determined according to the precise terms set out in it. This clearly included the respondent waterproofing the basement in accordance with the terms of the Contract.


B. Chronology of events ­ development of the design of the basement and waterproofing

52 In May 2006, Mr Psaros, at PPG, was provided with a geotechnical report prepared by Mr Davenport, then of Golder (Golder May 2006 Report), which advised, inter alia, of the following matters:


(Page 18)
    • The Perth Groundwater Atlas (1997) published by the Water and Rivers Commission shows the maximum groundwater level recorded at the location to be at approximately elevation RL 10.5 AHD.

    • The maximum groundwater levels were recorded prior to construction of the Graham Farmer Freeway tunnel. The presence of the tunnel and its associated drainage system may have a local influence on the groundwater level. Given that the groundwater flow is north to south across the site, mounding of the groundwater on the north side of the tunnel is a distinct possibility.

    • Fieldwork carried out on 11 and 25 April 2006 demonstrated, inter alia, that the approximate groundwater elevation at that particular time was between RL 9.2 AHD and RL 9.5 AHD.

    • The finished floor level of the basement carpark is proposed to be at elevations ranging from RL 9.4 AHD to RL 9.9 AHD.

    • These elevations are about 4 metres below ground level.

    • Based on historical groundwater information and groundwater elevations measured in the field, the maximum elevation of groundwater is likely to be at approximately RL 10.5 AHD.

    • The proposed basement carpark would be about 1 metre below the maximum level of the groundwater and subject to uplift pressure of about 10kpa.

    • Therefore, it is necessary to account for the uplift in design and construction. Failure to account for uplift pressure could lead to cracking of the basement slab and seepage into the basement.

    • Methods that could be used include:


      a) designing the base slab to resist uplift and partly tank the basement; and
(Page 19)
    b) drawing the groundwater level down to base slab level by installing an under drainage system to collect and channel groundwater to a sump for pumping into the street drainage system, or

    c) a combination of these methods.

    However, designing the base slab to resist uplift and tanking the basement is the only method which will not require ongoing operation and maintenance costs.


53 This 'sub drainage system' (or 'sub floor drainage system') is to be distinguished from the 'sub drainage relief system'.

54 The 'sub drainage relief system' is also called 'relief points' or 'relief vents'. The Tribunal will refer to the sub drainage relief system as 'the relief vents'.

55 Mr Psaros said in cross­examination that he was aware after having read the Golder May 2006 Report that, historically, groundwater had been as high as RL 10.5 AHD, and of the need to account for uplift pressure.

56 The Tribunal finds that, as from about May 2006, Mr Psaros knew that historical water levels had reached RL 10.5 AHD and of the need to account for groundwater uplift pressure.

57 To the extent that some of Mr Psaros' evidence was also contradictory (T:290­292; 12.10.12), the Tribunal does not accept that evidence, and prefers the aspects of Mr Psaros' evidence that accord with the documentary evidence.

58 On or around 20 July 2006, SEG issued plan S101 revision A and plan S102 revision A showing that the basement slab on the ground was to be 100 millimetres thick.

59 SEG plan S201 revision 1 and plan S202 revision 1 regarding 'concrete details' (Exhibit V, pages 120 and 121) issued on or around 12 October 2006 show that the slab on ground, including across control joints within the slab, and external face of the retaining walls, are to be waterproofed. The Tribunal concludes, as they have not been produced in compliance with the Tribunal's orders of 22 November 2012, that there were no Specifications at this time.

(Page 20)



60 Also on or around 12 October 2006, the Architects produced plan A101 revision 1 and plan A102 revision B showing the finished floor level for the lowest part of the basement carpark at the northern end of the basement as RL 9.8 AHD, with a small section at RL 9.75 AHD. These plans do not also detail that the trenches of the transformer room and switchboard room and the lift pit are below finished floor level, but the photographic evidence does establish this. The diagram at Exhibit B3, page 50 also usefully depicts relative levels in relation to the services in the basement.

61 These plans also show that the Tyne Square complex is bounded on three sides by Lindsay Street, Newcastle Street and Beaufort Street, and on the fourth side by a number of domestic residences.

62 The ground levels along each of the boundaries vary as follows:


    Lindsay Street boundary RL 12.26 to RL 15.00;

    Newcastle Street boundary RL 14.25 to RL 15.00;

    Beaufort Street boundary RL 13.22 to RL 14.25; and

    Residential boundary RL 12.26 to RL 13.22.


63 Therefore the lowest level of the basement is 5.25 metres below the highest boundary level, being at the junction of Lindsay Street and Newcastle Street, and 2.51 metres below the lowest boundary level, being at the junction of Lindsay Street and the residential boundary.

64 The lowest level of the finished floor level in the northern part of the basement is RL 9.75 AHD.

65 The Tribunal finds that the lowest level of the finished floor level of the basement carpark is approximately 0.75 metres below the maximum groundwater level recorded at the location. The Tribunal also finds that the finished floor level of the basement is approximately 0.75 metres below what the maximum elevation of groundwater could possibly be.

66 Mr Psaros said in cross-examination that he understood, after having read the Golder May 2006 Report, that the basement could be approximately one metre below the maximum groundwater level of RL 10.5 AHD (T:291; 12.10.12).

(Page 21)



67 The Tribunal finds that, as from about May 2006, Mr Psaros knew that the basement could be approximately 1 metre below the maximum groundwater level of RL 10.5 AHD.

68 To the extent that some of Mr Psaros' evidence was contradictory (T: 290-292; 12.10.12), the Tribunal does not accept that evidence and prefers the aspects of Mr Psaros' evidence that accord with the documentary evidence, including the Golder May 2006 Report.

69 Approximately one month earlier, on or around 15 September 2006, SEG had issued plan S101 revision B and plan S102 revision B showing the basement slab on the ground was to be 100 millimetres thick.

70 Then, on or around 28 September 2006, SEG issued plan S101 revision 0 and plan S102 revision 0 which showed for the first time a thicker 200 millimetre slab on ground in the lowest segment of the basement. The 200 millimetre slab on ground in the lowest segment of the basement remained in the plans issued by SEG on or around 12 October 2006 and the plans issued on or around 20 October 2006.

71 Mr Peter Grant Airey is a structural engineer retained by the applicant. Mr Airey is a director of Airey Taylor Consulting Engineers and Scientists. He obtained, relevantly, a Bachelor of Engineering in 1960 from the University of Western Australia. The Tribunal accepts Mr Airey as a competent, independent expert and credible witness and accepts his evidence.

72 Mr Airey expressed the view that a 200 millimetre basement slab, as depicted in plan S101 revision 0 and plan S102 revision 0 and revisions 1 and 2, is broadly in line with what he would expect to be an appropriate response to the predicted uplift conditions to which the basement slab would be subject in the event of the predicted high water levels occurring.

73 The Tribunal accepts Mr Airey's evidence in this regard.

74 In around September 2006, relief vents were not part of the design of the basement.

75 The Tribunal finds that, during September 2006, the design of the basement slab was increased in thickness from 100 millimetres to 200 millimetres to resist groundwater uplift pressure.

(Page 22)



76 Further, the Tribunal finds that at 28 September 2006, the plans reflected that the basement was designed to be completely impervious to groundwater ingress.

77 To the extent that Mr Psaros' evidence suggested that at this stage the basement was not designed to be completely impervious to groundwater ingress (for example, T:299­301; 12.10.12), the Tribunal does not accept it, and prefers the documentary evidence referred to above.

78 Despite having received the Golder May 2006 Report, Mr Psaros decided to undertake his own investigations into groundwater levels. By email dated 19 September 2006, Mr Psaros had indicated to Mr Swift that:


    Because of water stop to basement walls / concrete slab ­ No perimeter spoon drain is required. Water level is +/- 8.500 ­ basement floor is +/-9300 (Exhibit B16, page 244).

79 By email dated 22 September 2006, which is copied to others, Mr Psaros of PPG advised Mr Neil Crownie of the Architects, inter alia, that at the north­west boundary on Lindsay Street there was an 'AHD RL to water of 9.690' (Exhibit A, page 71) and to pass this information on to relevant consultants and discuss the implications.

80 By email dated 20 December 2006, which is copied to others, Mr Psaros of PPG provided revised measurements of groundwater levels to Mr Frank Saraceni for Mr Saraceni's 'info and action' (Exhibit A, pages 73 and 74). This showed groundwater levels variedin different parts of the site. The groundwater level near the north­west boundary on Lindsay Street was depicted as 'AHD 9.12' (Exhibit A pages 73 and 74).

81 On or around 1 December 2006, a spreadsheet titled 'Following list of action is required in order for cost saving to be made' was circulated, according to Mr Psaros at paragraph 54 of his witness statement, by him as representative of the Project Manager. This document included item 158 which asked SEG:


    What level has been used for water level design? Dwg S101 - why is slab on ground 200 thick? Why are we using N20 bars above PF1 2.4 x 2.4 x .6 footing?

82 On or around 13 February 2007, SEG issued plans S101 revision 3 and S102 revision 3 showing the segment of the basement slab in the northern part of the carpark that had previously been depicted

166 All of the experts, when asked in joint conference whether they had seen a relief vent system such as that in the Tyne Square basement, responded that they had not (T:59; 11.10.12). When Mr Psaros was asked in cross­examination if he had ever used a relief drain system in the slab of the buildings he had constructed, he replied that he had not (T:117; 11.10.12).

(Page 43)



167 The experts agreed on what would happen if all stormwater (that is, rainwater draining into the soakwells) was routed off site, including that groundwater will still ingress the basement, albeit with differences as to how often this will occur (Exhibit K1 - K9; T:68; 11.10.12).

168 The experts addressed the fact that there has been a 'dry sequence of years' (T:51; 11.10.12) and that data shows that between 1993 and 2012 the height of regional groundwater has not exceeded slab level (T:48 and 49; 11.10.12). The experts agreed this data could be underestimated (T:51 and 52; 11.10.12).

169 There were also varying opinions as to how likely it was that the historical maximum height of RL 10.5 AHD would ever be reached again. However, ultimately Mr Lundorf said:


    When we do designs, we design to the worst case, and that's where the design the slab and - the system here should be designed for the 10.5 because the system, the collection system, the pumps should be able to pump for that event, but it doesn't mean it's going to happen every year or every second year. (T:53; 11.10.12)

170 Mr Davenport agreed that RL 10.5 AHD was the correct level to design to, and that to design to less than that level would be remiss (T:77; 11.10.12).

171 There is no evidence of any water ingress to the southern half of the basement (for example, Exhibit B8, pages 10 and 11).

172 Accordingly the Tribunal finds that a cause of water ingress to the northern parts of the basement carpark at the times identified is rainfall running into the soakwells, which then leads to groundwater in the immediate vicinity of the soakwells rising up past the height of the basement floor.

173 The Tribunal also finds that, while it has not been established that regional groundwater, as distinct from groundwater in the immediate vicinity, has risen up past the height of the basement slab to date, there has been, and continues to be, a risk that regional groundwater will rise up past the height of the basement slab and ingress the whole of the basement carpark, even if all stormwater was routed off site.

(Page 44)



D. The areas of the northern part of the basement where water has ingressed and the extent of the problem

174 The applicant led evidence as to when and where water has ingressed the northern half of the basement, principally through Mr Jacques Curty Bernard Malie, Mr John Ogilvie Ullner and Mr Stephen Ronald Grose.

175 The report dated 19 September 2012 by Concrete Waterproofing (WA) Pty Ltd (Concrete Waterproofing), which is annexure 3 to the first of Mr Ullner's witness statements (Exhibit B1(a)), was admitted on the basis that no weight will be attributed to the opinions expressed therein, given that the author of the report was not called (T:51; 08.10.12), and the Tribunal has attributed no weight to the opinions.

176 Mr Ullner is the Director of JOU1 Pty Ltd, which is the company that owns commercial premises at Tyne Square, part of which is leased to Coles. Mr Ullner is also a member of the Council of Owners, being the governing body corporate of Strata Plan 52843 for Tyne Square. Mr Ullner is authorised to act on behalf of the Council of Owners in these proceedings. Counsel for the respondent tested the evidence of Mr Ullner. The Tribunal found Mr Ullner straightforward in cross-examination. The Tribunal accepts Mr Ullner as a credible witness.

177 Mr Malie works as a storeman at Coles at Tyne Square five days per week between approximately 7 am and 3.30 pm. He is also the proprietor of Malie Cleaning, a cleaning business which performs commercial and domestic cleaning, including the common areas of Tyne Square. He is also the caretaker of the building and provides a report once a month of anything identified to be in need of fixing. This does not include access to the Western Power transformer room, the sub-station room and the apartments (Exhibit B8). Counsel for the respondent tested the evidence of Mr Malie. The Tribunal accepts Mr Malie as a credible witness.

178 Mr Grose is and has been employed by Western Power for slightly over 30 years. He is a Distribution Systems Policy Engineering team leader, responsible for developing standards and policy in relation to how people safely connect to the Western Power network (Exhibit B4). His qualifications are in business - not engineering - although he has engineers working for him (T:100; 09.10.12). The Tribunal accepts Mr Grose as a credible witness.

(Page 45)



179 Mr Martens, Mr Airey, Mr Sebbes, Mr Watts, Mr Lundorf, Mr Collins, Mr Davenport, Mr Lucchesi and Mr Dixon agree that, in their opinion, water has ingressed the basement through both 'joints and relief points', but that no measurements have been taken to quantify the amounts from each source (Exhibits K1 - K9).

180 From the time Mr Malie commenced as caretaker of the Tyne Square building in approximately October 2009, he did not see any evidence of water ingress to the basement carpark until after a large hailstorm struck Perth on 22 March 2010 (Exhibit B8, page 3, paragraphs 13 and 14).

181 Mr Ullner first became aware of water ingress to the basement carpark around 18 August 2011 (T:67; 08.10.12).

182 The respondent submitted that, from the evidence before the Tribunal, it appears that on two occasions identified by Mr Malie, and one further occasion in August 2011 identified by Mr Ullner, water was found in the basement. The respondent further submitted that there is every basis to conclude that Mr Dash's evidence regarding the sprinkler damage was one of the occasions identified by Mr Malie.

183 The Tribunal does not accept these submissions.

184 The Tribunal finds, based principally on the photographic evidence as well as the joint answer by the experts to question 2 from the expert conference on 10 October 2012 at Exhibit K, that there has been groundwater ingress to the northern part of the basement through both relief vents and joints in the basement slab.

185 More specifically, based on the weight of:


    a) the photographic evidence; and

    b) the evidence of Mr Ullner, (excluding the whole report of Concrete Waterproofing, Mr Malie and Mr Sebbes,

    the Tribunal finds that groundwater has ingressed at least:

      • up through various joints in the northern area of the basement on at least around 30 July, 3 September, and 7 and 13 December 2011, including into storerooms and the lift 3 corridor; and
(Page 46)
    • through the joint between the basement floor and walls at various points on the northern perimeter of the basement on at least around 30 July, 3 September, and 3 and 7 December 2011.

186 The Tribunal accepts Mr Malie's evidence, principally at Exhibit B8, pages 10 and 11, as to where the photographs he took are located. The Tribunal also accepts Mr Ullner's evidence as to when each such photograph was taken, even though it was Mr Malie who took them. The basis of Mr Ullner's evidence as to the time of a photograph - as he explains in paragraphs 66 and 67 of his witness statement at Exhibit B1, pages 31 and 32 - is the date displayed in the 'properties window' of each photograph. The Tribunal has attributed weight to Mr Ullner's evidence as to dates, despite it being hearsay, because the Tribunal accepts that the dates are the dates that were displayed in the 'properties window' of each photograph, and these dates broadly correlate with Mr Sebbes' evidence as to rainfall events.

187 The Tribunal also finds, based principally on the weight of photographic evidence and Mr Grose's evidence, that groundwater ingress through unsealed cable entry points has occurred into the trenches in the transformer room and switchboard room, which are under the finished floor level of the basement.

188 The Tribunal does not accept Mr Psaros' evidence to the extent that it is inconsistent, because it was non-responsive to, and inconsistent with, what is apparent in the photographic evidence (T:364; 12.10.12) and was also inconsistent with later evidence he gave (T:366 and 377; 12.10.12).

189 The Tribunal infers from the location of the trenches below floor level, the close proximity to soakwells 1 to 8 and the mounding of groundwater that has been occurring in the vicinity of the soakwells, as well as the height Mr Grose describes the water to have reached in both trenches, that:


    a) water also entered the trenches in the transformer room and switchboard room through the joints between the basement floor and walls at the north and north­west perimeter; and

    b) water ingress to the trenches through both cable entry points and joints occurred at least around 30 July, 3 September, and 7 and 13 December 2011.


(Page 47)



190 It was not in dispute that water ingressed lift pit 3 through the base of the wall at the end of the corridor to lift 3 and up through the adjacent joint. Mr Dash also explained how the respondent attended to the defects in this location (T:383 and 384; 12.10.12). The photograph at Exhibit Q and Exhibit B1, page 125 (T:69; 08.10.12) shows these lift 3 repairs.

191 The Tribunal accepts Mr Ullner's evidence that he was advised that lift 3 had stopped working due to water ingress on 22 August 2011 (T:68; 08.10.12.).

192 Mr Ullner gave evidence to the effect that the cost of repairing the damage that has been caused to the mechanical system of lift 3 has been estimated at $22,157. This estimate has been made by the applicant's insurer. On the face of it, there does not seem to be any reason why this sum could not have been claimed by the applicant in this application. However, the applicant has not made a claim against the respondent in these proceedings for this sum, apparently on the basis that it has an insurance claim pending.

193 In terms of the extent of the problem that the water ingress has caused for the owners and residents of Tyne Square, there are two categories of problems. The first relates to the consequences of having water ingress to trenches, which carry electrical cabling, and potentially rising up to the level of the floors of the transformer room and switchboard room. Mr Grose states in his witness statement that water covered both high and low voltage cables to within 200 millimetres of the floor level and that any further rise to a level of the switchgear cabinets would have resulted in Western Power having to shut down power to the building. The Tribunal does not regard the fact that Western Power has not directed that anything be done (T:101; 09.10.12) as reducing the seriousness of having water ingress to trenches which carry electrical cabling and potentially rising up to the level of the floors of the transformer room and switchboard room.

194 The second category of problems relates to the loss of amenity and risks for the owners and residents of Tyne Square. The applicant led evidence regarding the nature of loss of amenity and risks through Mr Richard Machell, which was further clarified during Mr Machell's testimony.

(Page 48)



195 Mr Machell is, relevantly, a registered builder who has a Diploma in Building from TAFE. He is also a sessional member of the State Administrative Tribunal but has no personal, financial or social connection with any of the members sitting on this Tribunal (T:402; 06.12.12). Mr Machell's opinion was extensively tested in cross-examination. The Tribunal accepts Mr Machell as a competent, independent expert and credible witness.

196 Mr Machell's reports of 2 October and 9 November 2012 were admitted into evidence, although the Tribunal accords no weight to paragraph 3.14 of the 9 November 2012 report, as it could not be tested.

197 The Tribunal accepts Mr Machell's assessment that the inundation of water into the transformer room and electrical service ducts created dangerous conditions.

198 Mr Machell also gave evidence as to the rate water would ingress the basement if RL 10.5 AHD was reached; namely, up to seven litres a second.

199 In answer to a question put by the respondent to Mr Lundorf and Mr Dixon to describe the rate water would come into the basement if regional groundwater reached RL 10.5 AHD but the stormwater distribution did not lead to mounding, Mr Lundorf said there would be 'a low rate trickling in'. Mr Dixon said water ingress through the relief vents then would not be more than 'a litre a second', which would be like 'a bit more than you're going to get out of your shower' (T:63; 11.10.12).

200 The Tribunal finds that, if regional groundwater reached RL 10.5 AHD, water would ingress through the relief vents at, at least, one litre per second.

201 Further, the Tribunal accepts Mr Machell's evidence regarding the nature of loss of amenity and risks. This evidence included, in effect, that, as well as having to step through water - perhaps flowing water - from time to time, which is undesirable and may lead to slipping, the presence of water is associated with increased humidity which may lead to corrosion of metal elements within the basement (T:417; 06.12.12). While the degree of severity may differ depending on the precise rate of water ingress, the nature of the loss of amenity and risks, in essence, does not.

202 The Tribunal also accepts Mr Airey's evidence that corrosion within the AFS walls is now occurring (T:45; 11.10.12).

(Page 49)



E. The evidence as to 'a competent builder' with respect to the relief vents

203 Mr Machell also expressed an opinion in his report dated 2 October 2012, inter alia, that a competent builder would not have proceeded to build Tyne Square in a way which included the relief vents or, effectively, with the level of waterproofing that was used.

204 In response to Mr Machell's 2 October 2012 report, the respondent relied on the opinion of Mr Bradley Pike, dated 7 November 2012.

205 Mr Pike is the Manager Compliance at JMG Building Surveyors and has a Bachelor Building Surveying from Central Queensland University and a Municipal Building Surveyors Certificate of Qualification from MBSCQ. Mr Pike gave evidence that, as a building surveyor, his role is to determine that the design of a building, through the documentation and statements prepared by appropriately qualified persons associated with the design, and the construction of a building, through appropriate inspections and from the qualifications and statements prepared by appropriately qualified persons associated with the construction, meets the requirements of the Building Code and the Australian Standards.

206 In his written opinion dated 7 November 2012, Mr Pike states that the question as to whether a competent builder would have constructed the basement floor slab in the manner that the slab has been constructed, or what a competent builder should have reasonably done in this situation, is beyond his expertise. Mr Pike was called but was not subjected to cross­examination.

207 The Tribunal accepts Mr Pike as a competent, independent expert and credible witness. The Tribunal also accept the limits to Mr Pike's expertise.

208 The respondent did not provide a registered builder to provide an alternative perspective, or any other expert to respond to Mr Machell's opinion that a competent builder would not have proceeded to build Tyne Square in a way which included the relief vents, or which included the level of waterproofing involved.

209 The Tribunal does not accept the respondent's position that Mr Machell's opinion is invalid because it is provided with the benefit of hindsight, although careful regard must always be had to the basis upon which workmanship is being assessed.

(Page 50)



210 The Tribunal accepts that Mr Machell is qualified to provide an opinion regarding the relief vents and level of waterproofing.

211 However, the Tribunal has some difficulty with the relevance of the notion of 'a competent builder'. Even a competent builder may suffer an error of judgment. It must be borne in mind that the issue is whether the building service has not been carried out in a proper or proficient manner, or is faulty or unsatisfactory. As such, some of Mr Machell's evidence (in paragraphs 5.1 - 6.2.2 of his 2 October 2012) report does not directly address the issue that has to be determined in this case.

212 At paragraph 6.1.16, Mr Machell expresses the opinion that in respect of the installation of 15 floor wastes (meaning the relief vents) in the carpark as a solution to groundwater pressure, the concept provides a solution to the structural issues only, without consideration of the practical considerations of compliance with the other provisions of the Building Code. Mr Machell concludes that this would be immediately apparent to a competent builder faced with floor wastes in a basement, a site that required dewatering and had a maximum groundwater level of 10.5 AHD, with a floor installed at 9.8 AHD and in the absence of the sub drainage system.

213 The Tribunal accepts this aspect of Mr Machell's opinion.

214 The Tribunal finds that it was, or ought to have been, immediately apparent to Mr Psaros that, while the relief vents could resolve the issue of hydrostatic pressure on the basement slab, the installation of the relief vents would, in turn, create problems with the building.




F. What has now been done to date to remedy aspects of the problems

215 There are a number of steps that have been taken by the applicant and also by the respondent to remedy aspects of the problems.

216 In terms of the interim remedial steps undertaken by the applicant, Mr Ullner also gave evidence regarding such work performed.

217 This work included:


    a) the installation of solid block bunding to protect the switchboard room and transformer room and sewer pump from flooding;

    b) the installation of waterproof render and seals to bund walls;


Other Parts:Pages 51 to 86
wa.gov.au

Home | Privacy Information | Copyright and Disclaimer
All contents copyright Government of Western Australia. All rights reserved

Actions
Download as PDF Download as Word Document


Cases Citing This Decision

8

Cases Cited

8

Statutory Material Cited

11